HEAT UP TEST OF LONG WELDED RAIL ON SLAB TRACK
To study forces acting on slab track caused by thermal expansion of long welded rail or of the concrete slabs, heating tests were conducted on a newly built section. Special effort was made to eliminate residual forces at the beginning of the experiment. It was proved that longitudinal force caused by welded rail acting through the track fasteners is about 60 percent of the design value. Lateral force and distortion of the track is comparatively small.
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Availability:
- Find a library where document is available. Order URL: http://worldcat.org/oclc/3127232
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Corporate Authors:
Railway Technical Research Institute
Kunitachi, Box 9
Tokyo, JapanJAPANESE NATIONAL RAILWAYS
TOKYO, Japan -
Authors:
- Miura, S
- Publication Date: 1976
Media Info
- Features: Figures; Tables;
- Pagination: p. 86-87
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Serial:
- Railway Technical Research Institute, Quarterly Reports
- Volume: 17
- Issue Number: 2
- Publisher: Railway Technical Research Institute/Tetsudo Gijutsu Kenkyujo
- ISSN: 0033-9008
- Serial URL: http://www.rtri.or.jp/eng/
Subject/Index Terms
- TRT Terms: Buckling; Concrete slab track; Rail fasteners; Railroad rails; Railroad tracks; Structural design; Thermal stresses
- Uncontrolled Terms: Lateral loads; Track design
- Old TRIS Terms: Rail thermal stresses
- Subject Areas: Design; Railroads;
Filing Info
- Accession Number: 00142264
- Record Type: Publication
- Source Agency: Railway Technical Research Institute
- Files: TRIS
- Created Date: Nov 23 1976 12:00AM